That is a great story!
Now let me tell you what really happened.....
The front seater in the B model was coming off a six month grounding for discipline. He had a back seater IP with him for NVG requal. The pilot in the A model was ordered to fly this mission as his NVG intercept target. Straight and level at 14,000 feet and 300 KIAS. The front seater in the B model had threaten to Mid-Air the A model pilot. He made these statements in front of a squadron meeting and it was no secret. They had not flown together for sometime and the OGC ordered the pairing that night. The B model pilot intentionally rammed the single seat from behind and tried to commit suicide. After the collision, the B model lost its wing and exploded. The single seater flew rescap until his plane was falling apart. He RTB'd to nearset airstrip, ACY. He flew a deadstick approach at night, with a min controll airspeed of 220KIAS, to a runway with no approach lights, and a tailwind of ten knots. Before he left the cap, he was talking with a USCG helo pilot from brooklyn doing a night training mission. They were the first rescue asset on scene. The USCG scrambled a second helo from cape may. They had not moved to ACY yet. The First helo didn't have NVGs onboard, so they got the back seater who was competent and vectored them in. The front seater was hypothermic and in shock, the second helo used its night vision and located the front seater. A swimmer jumped in and saved him. Both helo crews did an outstanding job that night! The front seater was rushed to a trauma center and the helo with the back seater brought him to the F-16 base where an ambulance transported him to the couty general hospital. Both pilots never got a chance to see each other, although I'm sure the back seater would have kicked his ass all the way to the hospital!
After the USAF Safety Board completed its findings;
The wing commander was fired, the vice-wing commander was fired, the OGC was allowed to retire in disgrace, the squadron commander retired, and best of all......
the front seater was found to be mentally unfit and was stripped of his commission and thrown out! He was almost court martialed for attempted murder. Unfortunately, He had some incriminating evidence of very senior state officers doing very junior enlisted girls. He was given 12 hours to get out of sight! What is he doing now......
He is a Captain for United Airlines!
The IP in the back seat lied to the SIB and was found causal in the crash. The front seater got him a job at United. The single seater pilot was cleared in the crash by the SIB and then publically found partially at fault by the AIB. He was at 13,920 feet and 292 KIAS at impact. The slower than briefed speed contributed to the closure problem and was a factor in the crash. SWEAR TO GOD! He was hit by the D model doing over 520 KIAS. It was a very bad job of trying to cover it up and mitigate the damage to the NJANG.
I appreciate your version and never mind hearing all the interesting rumors of that night. Keep the stories coming.....