LXJ31
dirka dirka jihad dirka
- Joined
- Jan 15, 2002
- Posts
- 309
Ty Webb said:After all, he did "miss the runway on takeoff", you know.
LOL! Happens to the best of us....
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Ty Webb said:After all, he did "miss the runway on takeoff", you know.
LXJ31 said:See my previous post. When you say "Intentionally flying with a stuck elevator....sheeesh!," its minimizing what actually is occuring. Its not a simple choice, in some cases, of deciding that I'd enjoy the death-defying challenge of flying a malfunctioning airplane, or that I think aborted takeoffs are for quitters, but rather using one's head to analyze the situation before you even leave the chocks. .
Ty Webb said:Amen, and well-put. Evidently, what they did worked- a worst-case scenario and everyone lived. Hope they don't turn around and hang him in the court of public opinion. After all, he did "miss the runway on takeoff", you know.
Texasskicker said:NTSB Identification: NYC04IA054.
The docket is stored in the Docket Management System (DMS). Please contact Public Inquiries
14 CFR Part 91: General Aviation
Incident occurred Tuesday, December 16, 2003 in Teterboro, NJ
Probable Cause Approval Date: 12/3/2004
Aircraft: Canadair CL-600, registration: N95EB
Injuries: 2 Uninjured.
Earlier in the day, a different flightcrew performed a successful aborted takeoff in the incident airplane. The aborted takeoff occurred with seven to nine passengers on board, at 139 knots; when the flightcrew was unable to rotate the airplane. The only difference between that aborted takeoff, and the uneventful previous flight, was the addition of 3,000 to 4,000 pounds of fuel. Following that aborted takeoff, the airplane underwent a maintenance inspection which did not reveal any discrepancies pertaining to the inability to rotate. The airplane was then returned to service. When the incident captain arrived at the airport, he was informed of the previous aborted takeoff. The incident captain attempted a takeoff on a shorter runway at the airport. During rotation, the airplane did not respond to elevator inputs, and the captain aborted the takeoff. The airplane then traveled off the end of the runway and came to rest in mud. Following the overrun, the incident captain failed to produce a weight and balance calculation, or accurate count of passengers on board at the time. The wind was reported as variable at 4 knots. When asked why he chose a shorter runway to attempt the takeoff, the incident captain reported that it was the runway in use at the time. The aircraft manufacturer inspected the airplane, and did not find any discrepancies pertaining to the aborted takeoff. The manufacturer also computed two weight and balance calculations for the incident takeoff. Both calculations revealed that the airplane was above the maximum gross takeoff weight, and outside the forward center-of-gravity envelope. Subsequently, the airplane tookoff with no passengers on board, and flew uneventfully to another airport.
The National Transportation Safety Board determines the probable cause(s) of this incident as follows:
The captain's inadequate preflight planning, which resulted in an overrun during an aborted takeoff.
National Transportation Safety Board
Washington, DC 20594
Texasskicker said:Those of you who scoffed at my suggestion in the days right after this unfortunate accident occurred, now take heed. Remember, this is the 2003 accident data I quoted.
Here is what AIN is sayin'
Well forward’ C.G. Implicated in TEB Challenger Overrun
“The center of gravity (c.g.) was found to be well forward of the allowable limit,” according to an NTSB update of the investigation into the Challenger 600 that overran Runway 6 on takeoff from Teterboro Airport, N.J., on February 2. Initial findings of the investigation have indicated that the airplane, as configured, would have had a c.g.“well forward of the forward limit based on its cabin interior configuration combined with full or nearly full fuel tanks, including the fuselage tank, and a full or nearly full passenger load and minimum passenger baggage,” the NTSB said. In addition, the horizontal stabilizer trim position was in the middle of the green band (the normal takeoff range). The NTSB said it conducted tests using a simulator to evaluate the airplane’s takeoff characteristics based on the trim settings and weight-and-balance data. “The initial findings of those simulations indicate the airplane would not rotate for takeoff at the defined rotation speed.” The Safety Board also found that on the morning of the accident, icing conditions at Teterboro were “minimal or nonexistent” and there were “no anomalies” of the pitch-control system. A CVR transcript will be released in the near future. Meanwhile, the FAA revoked the Part 135 certificate of Darby Aviation (dba AlphaJet), one of the operators connected with the Challenger flight
Verified, Y'ALL.
Tx.
Publishers said:I knew the pilot of this aircraft and he is not one to cut any corners whatsoever, has a tremendous record, was a pilot for Pepsi and has recommendation from a number of his employers and customers.
He flew high profile government dignataries and believed safety first.
Vortilon breaks the first rule, it is ok to speculate on the cause but not on the pilots when you have no clue who the h they were.