Lopaka
4 string member
- Joined
- Jun 24, 2003
- Posts
- 77
We had just dropped off passengers in Treasure Cay, Bahamas and now were on our way to Ft. Pierce when we got the L chip det light. We monitored the guages nothing abnormal, everything constant and in the green when 10 min later the light flickered and went out. 15 sec. after that the torque needle dropped, and there went the engine. We were about 50 NM off shore but made it to Ft. Pierce just fine. The plane was towed to the turbine shop on the field where they pulled the chip detect plug and metal poured out of the engine. We're in the process of getting a loaner installed. Interesting thing (I guess) is, it's a '92 King Air 200 with the original engines. 2,620 hrs tt. Phase I-IV completed 200 hrs ago. I didn't think this was supposed to happen that often, but our sim instructor at FS said he's had twice. You think P&W will be interested in this case being original engines and almost 400 hrs from TBO? Worst part is we had to drive home, but now we've got a couple days off finally so we can fire up the barbi. That's pretty good, my first post and I already slipped in the BBQ thing. 